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Investigation and Control Technology on Excessive Ammonia-Slipping in Coal-Fired Plants.

Authors :
Yao, Xuan
Zhang, Man
Kong, Hao
Lyu, Junfu
Yang, Hairui
Source :
Energies (19961073). Aug2020, Vol. 13 Issue 16, p4249. 1p.
Publication Year :
2020

Abstract

After the implementation of the ultra-low emissions regulation on the coal-fired power plants in China, the problem of the excessive ammonia-slipping from selective catalytic reduction (SCR) seems to be more severe. This paper analyzes the operating statistics of the coal-fired plants including 300 MW/600 MW/1000-MW units. Statistics data show that the phenomenon of the excessive ammonia-slipping is widespread. The average excessive rate is over 110%, while in the small units the value is even higher. A field test data of nine power plants showed that excessive ammonia-slipping at the outlet of SCR decreased following the flue-gas process. After most ammonia reduced by the dust collector and the wet flue-gas desulfurization (FGD), the ammonia emission at the stack was extremely low. At same time, a method based on probability distribution is proposed in this paper to describe the relationship between the NH3/NOX distribution deviation and the De–NOX efficiency/ammonia-slipping. This paper also did some original work to solve the ammonia-slipping problem. A real-time self-feedback ammonia injection technology using neural network algorithm to predict and moderate the ammonia distribution is proposed to decrease the NH3/NOX deviation and excessive ammonia-slipping. The technology is demonstrated in a 600-MW unit and works successfully. The excessive ammonia-slipping problem is well controlled after the implementation of the technology. [ABSTRACT FROM AUTHOR]

Details

Language :
English
ISSN :
19961073
Volume :
13
Issue :
16
Database :
Academic Search Index
Journal :
Energies (19961073)
Publication Type :
Academic Journal
Accession number :
145285633
Full Text :
https://doi.org/10.3390/en13164249