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Failure Analysis and Experiment of Shale Gas Gathering Pipeline.

Authors :
Chen, Yong
Luo, Taiwei
Meng, Dongying
Wang, Qiliang
Tao, Xiao
Pu, Wenxin
Xie, Ruifei
Source :
Transactions of the Indian Institute of Metals; Nov2024, Vol. 77 Issue 11, p3641-3652, 12p
Publication Year :
2024

Abstract

This paper explores the reasons for the perforation failure of the shale gas gathering pipeline in the E Gas Mine and proposes preventive measures. EDS experiment found that the corrosion products were mainly Fe<subscript>2</subscript>O<subscript>3</subscript>, FeS, and FeCO<subscript>3</subscript>. Shale gas contains 24.908 g/m<superscript>3</superscript> CO<subscript>2</subscript> and 0.384 g/m<superscript>3</superscript> H<subscript>2</subscript>S, and formation water contains 20.445 g/m<superscript>3</superscript> Cl<superscript>−</superscript>. Therefore, CO<subscript>2</subscript>/H<subscript>2</subscript>S corrosion has occurred in the pipeline, and Cl<superscript>−</superscript> exacerbated localized damage to the material matrix, accelerated corrosion of the pipeline. The base material was more corrosion resistant than the weld, but the weld was more erosion resistant than the base material. The CFD simulation results found that the main reason of pipeline erosion is that, the shale gas contains grit and the gas volume exceeds the designed gas volume. So, the perforation failure of the pipeline was a result of both corrosion and erosion, and the effect of erosion is stronger than that of CO<subscript>2</subscript>/H<subscript>2</subscript>S corrosion on the pipeline. [ABSTRACT FROM AUTHOR]

Details

Language :
English
ISSN :
09722815
Volume :
77
Issue :
11
Database :
Complementary Index
Journal :
Transactions of the Indian Institute of Metals
Publication Type :
Academic Journal
Accession number :
180589481
Full Text :
https://doi.org/10.1007/s12666-024-03328-6