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First Successful Smart Liner Deployed in a Side-Tracked Gas Well, Offshore Abu Dhabi

Authors :
Abdelhak Mohamed Ladmia
Hamdan A Alhammadi
Dr. Elyes Draoui
Dr. Kristian Mogensen
Fahad Mohamed.M Al Hosani
Graham Edmonstone
Ahmed Mohamed Aldhanhani
Faisal Jamaan Ballaith
Ayman Mohamed
Navindran Juvarajah
Source :
Day 3 Wed, November 17, 2021.
Publication Year :
2021
Publisher :
SPE, 2021.

Abstract

This paper presents a summary of the deployed Smart Liner- SL equivalent to the Limited Entry Liner- LEL as lower completion for the first time in a sidetracked Gas well, Offshore Abu Dhabi. R-1 is subdivided into several sub-layers, the reservoir properties are characterized by low porosity & low permeability (Tight). Reservoir quality in the Upper part is better in terms of porosity & permeability than the lower part. The gas production is mainly from top part of R-1 reservoir, no contribution from Lower part. In 2017, Data gathering was conducted on well A-1 (Coring, Logging & Pressure Points). Actual Gas production Offset wells are restricted from optimal production due to Well Integrity Sustainable Annulus Pressure, to compensate the restricted aged wells due to Well Integrity, Gas production can be increased to 3 times using SL as a stimulation method.The Smart Liner was selected as a lower completion and as a stimulation method for better flow distribution, improved well performance, effective Acid stimulation, also to ensure hole accessibility, allowing aggressive bullhead stimulation at high rate/pressure and high acid concentration at less time ~ 1.5days/job, in addition to eliminating high risk and high cost Coiled Tubing (CT) intervention for stimulation.The first step was to design the SL Completion Workflow with a representative well trajectory for the selected well to be fed and reservoir properties to be extracted from the dynamic model, and then to create a representative stimulation model utilizing property numerical software with all possible scenarios; open hole that represents PPL and suggested SL compartmentalization and holes distribution based on reservoir parameters along the lateral. Once the well model is created, different scenarios for different completion designs are to be run versus different acid concentrations and volumes till achieving the optimum results from stimulation point of view in addition to formation and facilities limitations. Drilling operations were very challenging; fortunately, we succeed to deploy the SL after final adjustment based on FMI Natural Fractures. The Smart Liner as stimulation has proved to be a cost-effective solution for gas wells comparing to advanced stimulation methods in addition to eliminating the high risk and high cost of the Coiled Tubing (CT) intervention for stimulation a huge savings in well construction with maximizing performance.

Details

Database :
OpenAIRE
Journal :
Day 3 Wed, November 17, 2021
Accession number :
edsair.doi...........8e9a764b14ec0113199adc4f1fa75de9
Full Text :
https://doi.org/10.2118/207527-ms