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In-Situ and Laboratory Investigation on Leaching and Effects of Early Curing of Shotcrete

Authors :
Sjölander Andreas
Ansell Anders
Source :
Nordic Concrete Research, Vol 61, Iss 2, Pp 23-37 (2019)
Publication Year :
2019
Publisher :
Sciendo, 2019.

Abstract

During the construction of a rock tunnel in Stockholm, several sections with leaching shotcrete (sprayed concrete) were found one year after the spraying was completed. An investigation was therefore conducted, and its results are presented in this paper. The amount of leaching after such a short time indicated that a one-sided water pressure existed in combination with a permeable shotcrete. The reason for the water pressure was likely a partly unsuccessful grouting that created sections with leaking water. The permeable shotcrete could be a combined result of insufficient curing and the use of accelerators, and the effect of in-situ curing was therefore investigated. A total of six slabs were sprayed and cured under different conditions in the tunnel. Test results according to standards indicated that curing has no significant effect on the development of mechanical strength or water penetration through the shotcrete. However, this is believed to be a result of the test method rather than the non-existing effect of curing. Lastly, some modifications to the test standard were proposed for future studies of in-situ curing.

Details

Language :
English
ISSN :
25452819
Volume :
61
Issue :
2
Database :
Directory of Open Access Journals
Journal :
Nordic Concrete Research
Publication Type :
Academic Journal
Accession number :
edsdoj.8ddb139d77334c73b18f967a9e0d3ba9
Document Type :
article
Full Text :
https://doi.org/10.2478/ncr-2019-0014